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author | 2012-10-24 11:21:35 +0100 | |
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committer | 2012-11-01 13:02:26 +0100 | |
commit | 98c52c7c676b047e67c235616cc3fefad05c04d4 (patch) | |
tree | 87942c63ef514ed0531a4e0783de31ae0bb992e7 /tools/perf/scripts/python/export-to-postgresql.py | |
parent | ARM: ux500: Add node for the MMC GPIO regulator (diff) | |
download | linux-dev-98c52c7c676b047e67c235616cc3fefad05c04d4.tar.xz linux-dev-98c52c7c676b047e67c235616cc3fefad05c04d4.zip |
ARM: ux500: Change the type of interrupt to something compatible
On boot the Nomadik GPIO controller complains that an IRQ can't be
configured as active high level-sensitive, so this patch converts
it to be low-to-high edge triggered instead.
Acked-by: Linus Walleij <linus.walleij@linaro.org>
Signed-off-by: Lee Jones <lee.jones@linaro.org>
Diffstat (limited to 'tools/perf/scripts/python/export-to-postgresql.py')
0 files changed, 0 insertions, 0 deletions